metaruss

Archive for July, 2008

The Daytona: July 29, 2008

by on Jul.29, 2008, under Daytona

A week or two after the convention, the car suddenly got a bad vibration when making right turns.  It seemed like the left axle tripod was bottoming-out.  I had recentered the engine when I had the old stock axle in there and never put it back, but I wasn’t sure what caused it to suddenly appear one day.  It turned out that the aftermarket trans mount I installed had partially collapsed, which was enough to take out the last bit of slack in the axle.  Anyway, I put the poly trans mount back in (the engine vibrations were no better with the rubber mount anyway), fixed the front mount bracket so I could slip washers in there to space the poly away from the bracket, and recentered the engine.  Everything is fine now and the washers did seem to help a bit with the vibs.

I also cleaned-up the crab rims from the CSX, hit the lips with a scotch-brite abrasive wheel, and polished them a bit before installing them on the Daytona.  The Dunlop SP8000s from JT are worn down to the markers now, so I’m running the Kuhmo 712s from the CSX.  They have flat spots from the freeway spin-out, but they do have plenty of tread.  The Dunlops were awesome tires, but you can’t get them in 225/50 R15 anymore.  I’m saving the last of them for the CSX when it is done.

Lastly, I made shims for the brake pads on all four calipers to try to shut them up.  They still squeak, but are better overall.  I think the notches that are worn into the brackets from the pad plates may be to blame.  Would have to weld them up somehow, but I have bigger fish to fry.

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The Daytona: July 9, 2008

by on Jul.09, 2008, under Daytona

The first time I drove the car after coming home from the convention, the door handle broke on the drivers side.  Joe from the club was nice enough to pick one up from an 85 Daytona in the junkyard and ship it to me.  The rod had to be bent to match the old one, but it swapped over just fine otherwise.  While the door was apart, I installed the ’87 power mirrors.  Man, the ’91 wiring diagrams are horrible.  Not one single interesting circuit on the power mirror page was right and as such my splice job from way back when did not work.  I spent many hours trying to sort that out, but now I finally have working power mirrors!

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Blueberry 60.16

by on Jul.07, 2008, under Blueberry

07/07/2008: Version 60.16 (based on “Blueberry60”) – Revert ColdEnrichmentFuelCurveA back to stock since AIS changes seemed to address part of lean startup conditions. Remove more timing from AdvanceFromMapWarmFull to widen range down to -2psi.

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Blueberry 60.15

by on Jul.03, 2008, under Blueberry

07/03/2008: Version 60.15 (based on “Blueberry60”) – Increase boost goals/limits to 21psi. Fix lots of missing TBL entries and re-enable staging mod. Get rid of “2bar/3bar” table names to permit easier comparisons to Turbonator and stock cals. Revert AIS tables and FuelLeanoutFactorOffThrottle back to stock. Bump FuelMonitorScaling to compensate for observed fuel useage discrepencies. Retard timing between 0 to 15psi up to -10 degrees at 6psi in AdvanceFromMapWarmFull for improved turbo spool.

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