metaruss

Daytona

No more MacGyver chair

by Russ on Oct.09, 2009, under Daytona

Re-rewelded the driver’s seat frame. It was broken into three pieces and was being held in place by an empty cat litter container. I added some steel to it, so I don’t expect it to break again, at least on in that spot. The bottom cushion has a weird feel to it now, probably because it is being properly supported for the first time in years.

The UltraFlo muffler rusted-off. That thing only lasted 3 years…not impressive. Put the Super Turbo back on there…it’s no quieter than the UltraFlo (at least on the inside), but maybe it’s quieter for the neighbors.

The water pump housing has been leaking for years, but now coolant is dropping at an alarming rate. Not sure if it was the leak or something else, but the housing is now resealed. The car suddenly started using more oil than before as well, so something is clearly amiss. Last time I had the turbo intake off, I saw oil in there. There is still a very small amount of oil in the coolant. Now sure if it’s just leftover film or if there is a leak or crack somewhere. I’m guessing that I will find out sooner or later what the issue is/are.

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A/C Again

by Russ on Jul.01, 2009, under Daytona

I haven’t done anything to this car since last July other than drive it. It’s been daily driven for an entire year. 3rd gear is still jacked-up, but got a little better over time until recently. Now I can hardly get it in, but I can say that it is the shift pads again. 4th is starting to give a little trouble too, so I think I will swap the whole 3-4 gear pack for one from an ‘89 A555. I wish I could buy new stop rings for less than the cost of an entire transmission. That damn short DSS axle ripped through it’s inner boot again, this time it wore through the inside. Aside from being shoddily assembled, they obviously don’t intend anyone to use these on the street. Pretty lame, given what they cost. This time the spring broke inside the tripod, probably because it can’t sit flat on the shaft end due to those welds.

Last week was really hot, so that motivated me to try to fix the A/C. Had to fix the air compressor first and various other things, but finally got it done. There was a slow leak at the H-valve due to a poorly machined surface on the hoses. Crappy aftermarket parts. The compressor has been holding up so far, so we’ll see if it makes it through the summer. I would be impressed.

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The Daytona: July 29, 2008

by Russ on Jul.29, 2008, under Daytona

A week or two after the convention, the car suddenly got a bad vibration when making right turns.  It seemed like the left axle tripod was bottoming-out.  I had recentered the engine when I had the old stock axle in there and never put it back, but I wasn’t sure what caused it to suddenly appear one day.  It turned out that the aftermarket trans mount I installed had partially collapsed, which was enough to take out the last bit of slack in the axle.  Anyway, I put the poly trans mount back in (the engine vibrations were no better with the rubber mount anyway), fixed the front mount bracket so I could slip washers in there to space the poly away from the bracket, and recentered the engine.  Everything is fine now and the washers did seem to help a bit with the vibs.

I also cleaned-up the crab rims from the CSX, hit the lips with a scotch-brite abrasive wheel, and polished them a bit before installing them on the Daytona.  The Dunlop SP8000s from JT are worn down to the markers now, so I’m running the Kuhmo 712s from the CSX.  They have flat spots from the freeway spin-out, but they do have plenty of tread.  The Dunlops were awesome tires, but you can’t get them in 225/50 R15 anymore.  I’m saving the last of them for the CSX when it is done.

Lastly, I made shims for the brake pads on all four calipers to try to shut them up.  They still squeak, but are better overall.  I think the notches that are worn into the brackets from the pad plates may be to blame.  Would have to weld them up somehow, but I have bigger fish to fry.

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The Daytona: July 9, 2008

by Russ on Jul.09, 2008, under Daytona

The first time I drove the car after coming home from the convention, the door handle broke on the drivers side.  Joe from the club was nice enough to pick one up from an 85 Daytona in the junkyard and ship it to me.  The rod had to be bent to match the old one, but it swapped over just fine otherwise.  While the door was apart, I installed the ‘87 power mirrors.  Man, the ‘91 wiring diagrams are horrible.  Not one single interesting circuit on the power mirror page was right and as such my splice job from way back when did not work.  I spent many hours trying to sort that out, but now I finally have working power mirrors!

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The Daytona: June 26, 2008

by Russ on Jun.26, 2008, under Daytona

Another awesome time at SDAC has come and gone.  The performance driving school was a blast as always.  The Daytona did great overall, but the stress did highlight some issues.  The intercooler definitely needs to be kicked-out at the bottom to allow some air to get around it.  The loss in cooling capacity was very obvious after a few laps, though it will happen on the street in traffic with the A/C on as well.  I’m thinking of buying a new fan as well.  The other issue was oil pressure.  I know the pump has issues and when the oil temps got high, I was seeing only about 30psi of pressure at 5000rpm.  Not good, so I think it’s time for a new pump.

I made 14 passes at the drag strip.  Times weren’t what I had hoped (was shooting for 13s), but I didn’t break the car.  I couldn’t get the car to hook nor could I get it to make more than 18-19psi of boost…even with the wastegate unplugged.  I also trashed 3rd gear by the end and it seems that it will need a new syncro.  Did a bit of tuning, but most of the effort was spent trying to learn how to launch the car.  Best time was 14.269sec @ 98.87mph.

React 60′ 1/8 ET 1/8 MPH 1/4 ET 1/4 MPH Comments
0.659 2.757 11.049 70.65 16.261 94.11 First run. Completely borked the launch and then missed 3rd.
0.277 2.669 9.949 77.33 14.896 95.98 Swapped to BB60.14 cal. Slightly better launch. Hot-lapped.
0.634 2.654 9.923 76.15 14.894 96.78 Hot-lapped.
0.253 2.717 10.060 74.62 15.094 95.95 Crappy launch. Hot-lapped.
0.590 2.544 9.968 75.76 14.904 94.35 Hot-lapped.
0.494 2.620 9.899 75.60 14.803 102.99 Added boost to the cal.
0.510 2.498 9.792 75.12 14.732 99.98 Switched to grainger and dropped tire pressure to 35psi. Ended up with 15psi of boost.
0.514 2.364 9.380 76.51 14.275 100.08 Cranked up boost to 17psi.
0.339 2.437 9.674 75.63 14.598 100.19 18-19psi of boost. Best MPH.
0.145 3.092 10.719 74.40 15.686 99.53 Bumped trans out of 1st during launch.
0.261 2.265 9.276 73.87 14.269 98.87 Finally a decent launch. Best ET.
0.260 2.525 9.917 72.34 14.968 98.04 3rd grinding bad.
0.371 2.698 13.899 47.47 22.392 54.02 Turtle race (lost).
0.159 2.410 9.792 76.13 14.802 95.75 3rd is done.
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The Daytona: June 21, 2008

by Russ on Jun.21, 2008, under Daytona

So I’m going to SDAC-18 and have been doing a mad-dash to get the car ready.  The axle boot was the wrong one and tore itself up on the trans case.  I put an old stocker in there from the Shadow while I worked on other things.  Later I got the correct boots from JT and completely went though the axles.  Only the short axle has the tripod welded to it and it looks like they did it while the bearings were on.  They must have slipped and tagged one of them with the welder.  The tulip race is chewed-up pretty good there.  The outer joints have a lot of hammer blows on them and long axle’s has a lot of play and binds much beyond the center.  I put them back together anyway and they seem to be holding up so far.  I don’t expect to get a whole lot of miles out of them.

Trying to address the somewhat-weak oil pressure issues, I pulled the pan and removed the pickup.  My thought was that it may have been leaking at the o-ring since I had to bend the tube a bit when putting the motor together.  I took the pump apart as well to check the clearances.  It had a lot of scoring in it for some reason, but the clearances were all well within spec.  I also plastiguaged the rods bearings, which looked great and were nice and tight.

I’m going to be running the road course, so I put new pads and rotors in the front and bled the brakes.  Also replaced the front swaybar bushings with new ones from Johnny.  The radiator was throughly flushed, since I had some oil in there.

The ends on the CS Racer panhard bar were shot, so I modified a stocker to make it adjustable.  One end was cut off and a grade 10.9 M16 bolt welded to it.  Some of the bar was removed and an M16 coupler nut was welded to that end and the whole bar was boxed-in.  It warped a bit after all the welding, so I lowered on car on it to bend it straight again.  It was installed with new poly bushings from Johnny Spiva.

I DA’ed and rattle-canned the roof and mounted the side door mouldings.  Painted those as well as some missing paint on the nose.  Also painted the exposed bumper support since the grill is missing there.  Did lots of touch-ups and also tried to deal with the worst of the rust on the hood.  Didn’t have enough time to finish sanding and rubbing-out the patches, but it looks better than it did before.

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The Daytona: May 23, 2008

by Russ on May.23, 2008, under Daytona

Last night/this morning I finally fixed a few pressing issues.  One was the boot on the driver’s inner CV joint had chewed through itself a while ago and I’ve been meaning to put a new one one there for some time.  I discovered that the Driveshaft Shop Level 3 axles have the tripods welded to the shafts, so they have to be taken apart from the outer CV end.  Also, the inner joints have some kind of fiber reinforced plastic cap that seems to be there to keep the tripod in the tulip housing.  The problem is the boot seals to the cap and the cap seals to the tulip with a rubber seal.  On the other axle, grease is coming out between the cap and the tulip, so I am going to have to deal with that at some point..

The big project was replacing the shift fork pads on the 1-2 and 3-4 forks.  I’ve been limping 3rd gear along for over a year now, as I cheezed it pretty bad on a hard shift one day but it was still usable.  A week or so ago I did the same to 2nd gear, rendering it useless.  I hoped it was just the pads and so I bought some new ones.  Thankfully, that’s all it was.  The trans looked clean inside, though the sprags for 3rd and especially for 2nd gear are pretty chewed up.  It shifts great now, so I am not going to worry about it.

Finally, both of the outer tie rod ends are so sloppy that they have about 1/2″ of play now.  They are only a few years old, so no more Moog suspension parts for me.  I got the more expensive ones from NAPA (Spicer I think).  Same brand as the new ball joints that replaced the failed Moog joints and are holding up well.

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The Daytona: April 23, 2008

by Russ on Apr.23, 2008, under Daytona

Still my daily driver.  Been collecting some odds and ends that should hopefully help the spool department:  A Turbos Unleashed cast log header and Turbonetics T03/T04E hybrid single ball bearing turbo with a “Super 50″ compressor and a Stage II exhaust turbine in a .63 A/R housing attached to a Turbos Unleashed 3″ swing valve (whew).  The header, housing, and swing valve are all ceramic thermal coated to keep temps down and gas velocities high.  The turbo flange on the header is larger than it should be, so I will likely need to port the housing flange somewhat.


The Super 70 and ported exhaust manifold that is in there now will end up in the CSX once I get a new cylinder head for it.  Trouble is the CSX needs to be running before I put this setup in there….

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The Daytona: June 5, 2007

by Russ on Jun.05, 2007, under Daytona

Drove the car all winter and spring without any major issues.  The most annoying thing that happened was when the adjustable cam sprocket came loose and the car wouldn’t start late at night in the parking lot at work.  I was able to snug it up with some vice grips and get home.  I’ve got a stock sprocket on there now.

I recently replaced the stock headlamps with a Hella H4 “Free Form” conversion kit and built a relay module so that the lights got power directly from the battery.  I measured an over 3.5V drop through the stock headlight circuit.  The housings are DOT approved and I am using the standard 65/55W bulbs.  The light pattern is much better than a standard sealed-beam lamp and they run nice and bright with the extra voltage.  If you are thinking about a HID conversion for better visbility (and not because you think they are pretty), do the H4 conversion and relay mod instead.  The on-coming drivers will thank you (I hate HIDs).

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The Daytona: November 8, 2006

by Russ on Nov.08, 2006, under Daytona

The stupid cheesy plastic draincock on the brand new radiator broke on the way to work.  Stuffed a rag in the hole and limped back home.  What a crappy design.  Anyway, I did a few other odds and ends while I was at it, including the installation of the correct throttle cable.  I also got the interior all cleaned up nice and managed to take some pics of the inside and the outside (it’s a little dirty on the outside, but oh well).


I’m really happy with how the guage pod and mounts turned out.

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